Today we focused on building a working drive base. Although other sub-teams worked on their own systems, the main priority was making something that drove around. Unfortunately, we were unable to meet our goal due to wiring and mechanical issues. We hope to finish the working drive base by Monday.
Other sub-teams made progress, however. Intake replaced motors with more powerful ones. Climber worked on mounts for their systems. And lift…I’m not sure what lift did, but it was probably productive.
GO ROBOTOTES!!!