Today's meeting in two words: Practice and Autonomous.
A session of drive practice (thanks again to NRG for letting us use your practice field!) was sandwiched between debugging autonomous. However, if today were a sandwich, it would have some very moldy bread, with some slightly less moldy meat in between.
Needless to say, autonomous testing didn't work that well. The biggest issue is consistently putting the gear on the peg.
Meanwhile, the drive team practiced driving. The biggest problem is picking up the gear when the drive team can't even see it.
We only have one meeting left before Stop Build Day. This team has already gone crazy. Let's just hope we'll be sane enough to fix the robot tomorrow.